2002 T28 Summer projects
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Date |
Flight# |
Testing device |
Time |
Comments(location for test) |
Feb
5 |
Ground test |
Static/Pitot Pressure Calib |
|
Data
in C:\t28\yr2002\f799\pressure.raw Static
= 4000 ΰ 22,000 ft Pitot = 60 kt 180 kt Stat_press_1
= dn1*1.58675e-2 + 527.918 Stat_press_2
= dn2*1.09126e-2 + 694.525 |
Feb
6 |
Ground test |
Electrostatic testing on the T28 |
|
- consultant was Jack Chapdelaine -
sensitive points found at RFT, comm1 antenna and VOR
antenna. All
were remedied. |
April
19 |
F775 |
Instruments on T28 2DC HVPS Slow
data Hail
DMT FSSP |
In flight |
Pilot: Charlie Summers Data
in C:\t28\data\yr2002\f775\f4191336.raw -
536 buffers: good images, mostly ice -
0 buffers; non-charge mode -
2171 buffers: OK -
0 buffers: -
worked ok - did not work! Flight was short, mainly to check the brakes. Telemetry worked OK. No heading! |
April
25 |
Ground test |
Instruments on T28 2DC @ HVPS @ 15:10, 11 Slow
data Hail
DMT FSSP
@ |
Ground |
Balloon
on Pitot tube Water spray test. Data
in C:\t28\yr2002\backup\SDSMT\f4251457.raw C:\t28\yr2002\testf\f900\* -
recorded ok images -
recorded images -
ok - N/A |
May
3 |
F776 |
Instruments on T28 2DC HVPS Slow
data Hail
DMT FSSP |
In flight |
Pilot: Data
in C:\t28\data\yr2002\f776\f5031551.raw
5056 buffers: good images
6093 buffers; non-charge mode, collects 10 buffers/sec!;
some good buffers and lots of bad ones.
4745 buffers: ok -
194 buffers; good images. - worked ok. -
not working! Telemetry
worked ok. - FM test - P-static when in precip Due to lack of microphone for oxygen mask, pilot did not wear a
mask and flight was conducted at altitudes below 14 kft.
Precip was mainly small ice particles falling as virga. |
May
15 |
|
|
|
Donna
uses tag 17 (before used for heading) to retrieve NO data from the NOx analyzer. New Heading Card (INS synchroheading). For the new heading card create tag #990. |
May
20 |
|
|
|
|
May
21 |
Ground test |
|
|
File:
f5211127.raw Routine
get_heading2.pro includes the equations valid for the new heading card. |
May
22 |
Ground test |
|
|
File:
f5221507.raw; the heading plot was ok! |
May
23 |
F777 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx FSSP |
In flight |
Pilot: Tom Root 1st flight with TEI 42C-TL NOx
analyzer installed. Initially some trouble getting computer to boot. Data in: c:\t28\yr2002\f777\f5231833.raw -
0 records -
829 buffers: lots of bad buffers (stuck bit case) -
2333 buffers: ok -
0 records -
did not record any significant data -
very small readings (up to 1 ppbv) -
it worked this time |
June
3 |
F778 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx FSSP |
In flight |
Pilot: Tom Root Data
in: c:\t28\yr2002\f778\f6031811.raw - 176 buffers: ok - 113 buffers: but no
images, housekeeping does not look good -
6481 buffers: ok -
5 buffers: not really anything recorded. -
ok -
off -
Bad transformer in FSSP took to DMT for repair |
June
5 |
F779 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx FSSP |
|
Pilot: Charlie Summers Data
in : c:\t28\data\yr2002\f779\* -
no records - 1936 buffers: bad images -
2552 buffers: ok -
no records - ok -a spike value at -ok Transponder fails Fuel boost pump fails |
June
7 |
Ground test |
NOx analyzer |
Ground
test with all instruments on |
Calibration
for NO. File:
f6071605.raw Raw
file looks ok; HVPS
images look ok. 2DC
images look ok. |
June 9 |
F780 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx |
In flight |
Pilot: Charlie SummersData
in : c:\t28\data\yr2002\f780\* -
18 buffers with small particles in it. -
3015 buffers: all bad images. -
-
Donna adjusted HVPS image on the horizontal axes (x2) -
1798 buffers: ok -
none -
OK Note: Strong fires SW of Denver; could see the smoke; Charlie flew close to area of smoke, and NOx instrument had ~ 40 ppbv reading! |
June 10 |
|
Instrumentation tests in hangar |
|
Verified NO analyzer response at 43 and 90 ppbv Wired new switch for turning on analyzer in flight |
June 11 |
F781 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx FSSP |
In flight |
Pilot: Charlie Summers Data
in: c:\t28\data\yr2002\f781\f6120025.raw -1642
buffers: good images -
2266 buffers: some good buffers and some not good -
4970 buffers: ok -
620 buffers: looking good -
nothing recorded Donna I noted
a response during taxi after landing. So the instrument must have been on? -
working good NOx analyzer warm up test ~ 30 minutes to settle to 1
ppbv. Contacted SPEC to sent copies of the bad buffers we recorded with HVPS and ask their opinion in how to fix the problem. |
June 12 |
F782 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx FSSP |
In flight |
Pilot: Data
in: c:\t28\data\yr2002\f782\f6122351.raw -
249 buffers: good images -
3196 buffers: some good images, and many bad buffers -
2640 buffers: ok -
2 buffers: nothing there -
ok -
ok -
ok |
June
15 |
F783 |
|
|
Attempted to fly T28 from Pilot: Tom Root Pilot
noticed the chip light on, so he had to go back to |
June
15 |
F784 |
Instruments on T28 all off |
In flight |
Flight back to Pilot : Tom Root |
June 16 |
F785 |
Instruments on T28 2DC
HVPS
Slow
data Hail DMT NOx |
In flight |
Pilot: Charlie Summers Data
in:
c:\t28\data\yr2002\f785\f6162211.raw -
338 buffers: good images -
4707 buffers: some good images, and lots of bad ones -
3696 buffers: ok -
99 buffers: good images -
ok - Nice spike from nearby lightning at Flight terminated unexpectedly due to oil loss (2 gallons of
oil). Oil loss seemed to coincide with
switch to high blower. |
June
18 |
F786 |
Instruments on T28 |
In flight |
Pilot: Tom Root Pilot found a crack in the engine through which the oil
was lost. |